LTC3603
16
3603fc
For more information www.linear.com/LTC3603
applications inForMation
Choose a standard value of R2 = 475k. The voltage on
the MODE pin will be set to 0.6V by tying the MODE pin
to the FB pin. This will set the burst current equal to ap
-
proximately 1A. Figure 6 shows a complete schematic for
this design example.
How to Reduce SW Ringing
As with any switching regulator, there will be voltage
ringing on the SW node, especially for high input voltages.
The ringing amplitude and duration is dependent on the
switching speed (gate drive), layout (parasitic inductance)
and MOSFET output capacitance. This ringing contributes
to the overall EMI, noise and high frequency ripple. One
way to reduce ringing is to optimize layout. A good layout
minimizes parasitic inductance. Adding an RC snubber
from SW to GND is also an effective way to reduce ringing.
Finally, adding a resistor (10Ω to 100Ω) in series with the
BOOST pin will slow down the MOSFET turn-on slew rate
and dampen ringing, but at the cost of reduced efficiency.
Note that since the IC is buffered from high frequency
transients by PCB and bondwire inductances, the ringing
by itself is normally not a concern for reliability.
PC Board Layout Checklist
When laying out the printed circuit board, the following
checklist should be used to ensure proper operation of the
LTC3603. Check the following in your layout:
1. A ground plane is recommended. If a ground plane layer
is not used, the signal and power grounds should be
segregated with all small-signal components returning
to the SGND pin at one point which is then connected
to the PGND pin close to the LTC3603.
2. Connect the (+) terminal of the input capacitor(s), C
IN
, as
close as possible to the PV
IN
pin. This capacitor provides
the AC current into the internal power MOSFETs.
3. Keep the switching node, SW, away from all sensitive
small-signal nodes.
4. Flood all unused areas on all layers with copper. Flooding
with copper will reduce the temperature rise of power
components. You can connect the copper areas to any
DC net (PV
IN
, INTV
CC
, V
OUT
, PGND, SGND, or any other
DC rail in your system).
Figure 6. 12V to 3.3V, 2.5A Regulator at 1MHz, Burst Mode Operation
C
IN
22µF
V
IN
12V
V
OUT
3.3V
2.5A
3603 F06
D1
L1
2.2µH
R
OSC
105k
R
ITH
4.32k
R1
105k
R
PG
200k
L1: VISHAY IHLP2525CZER2R2MO1
C
IN
: TAIYO YUDEN TMK325BJ226MM-T
C
OUT
:
TDK
C3225X5ROJ107M
C
VCC
F
C
ITH
1nF
C
OUT
100µF
SYNC/MODE
PGOOD
RT
ITH
V
FB
RUN
TRACK/SS
PGND
INTV
CC
PV
IN
PV
IN
BOOST
SW
SW
SW
PGND
PGND
LTC3603
R2
475k
C
BST
0.22µF
PGOOD
C
FB
10pF
LTC3603
17
3603fc
For more information www.linear.com/LTC3603
typical applications
1.8V, 2.5A Regulator at 1MHz, Burst Mode Operation
1.2V, 2.5A Regulator at 750kHz, Burst Mode Operation
C
IN
22µF
V
IN
12V
V
OUT
1.8V
2.5A
3603 TA02
D1
L1
H
R
OSC
105k
R
ITH
4.32k
R1
105k
R3
845k
C
VCC
F
C
ITH
1nF
SYNC/MODE
PGOOD
RT
ITH
V
FB
RUN
TRACK/SS
PGND
INTV
CC
PV
IN
PV
IN
BOOST
SW
SW
SW
PGND
PGND
LTC3603
R
PG
200k
R4
137k
R2
210k
C
FB
10pF
C
OUT
100µF
× 2
C
BST
0.22µF
PGOOD
L1: VISHAY IHLP2525CZER1R0MO1
C
IN
: TAIYO YUDEN TMK325BJ226MM-T
C
OUT
:
TAIYO YUDEN
AMK316BJ107ML
C
IN
22µF
V
IN
12V
V
OUT
1.2V
2.5A
3603 TA03
D1
L1
H
R
OSC
143k
R
ITH
4.32k
R1
105k
R
PG
200k
C
VCC
F
C
ITH
1nF
SYNC/MODE
PGOOD
RT
ITH
V
FB
RUN
TRACK/SS
PGND
INTV
CC
PV
IN
PV
IN
BOOST
SW
SW
SW
PGND
PGND
LTC3603
R3
845k
R4
137k
R2
105k
L1: VISHAY IHLP2525CZER1ROMO1
C
IN
: TAIYO YUDEN TMK325BJ226MM-T
C
OUT
: TAIYO YUDEN AMK316BJ107ML
10pF
C
OUT
100µF
×2
C
BST
0.22µF
PGOOD
LTC3603
18
3603fc
For more information www.linear.com/LTC3603
typical applications
3.3V, 2.5A Regulator, Synchronized to 1.8MHz, Small Size
C
IN
22µF
V
IN
12V
V
OUT
2.5V
2.5A
3603 TA05
D1
L1
H
R
OSC
69.8k
R
ITH
2.94k
R1
105k
R
PG
200k
C
VCC
F
C
ITH
470pF
SYNC/MODE
PGOOD
RT
ITH
V
FB
RUN
TRACK/SS
PGND
INTV
CC
PV
IN
PV
IN
BOOST
SW
SW
SW
PGND
PGND
LTC3603
R2
332k
C
FB
10pF
C
OUT
47µF
C
BST
0.22µF
PGOOD
1.8MHz
EXT. CLK
L1: VISHAY IHLP2525CZER1ROMO1
C
IN
: TAIYO YUDEN TMK325BJ226MM-T
C
OUT
: MURATA GRM31CR60J476ME19
Efficiency vs Load Current,
1.8V Regulator at 1MHz, Burst Mode Operation
LOAD CURRENT (A)
70
EFFICIENCY (%)
80
85
95
100
0.001 0.1 1 10
3603 TA04a
60
0.01
90
75
65
V
IN
= 7.2V
V
IN
= 12V
Efficiency vs Load Current,
1.2V Regulator at 750kHz, Burst Mode Operation
LOAD CURRENT (A)
65
EFFICIENCY (%)
95
60
55
90
75
85
80
70
0.001 0.1 1 10
3603 TA04b
50
0.01
V
IN
= 7.2V
V
IN
= 12V

LTC3603EUF#PBF

Mfr. #:
Manufacturer:
Analog Devices / Linear Technology
Description:
Switching Voltage Regulators 2.5A, 15V Mono Sync Buck Reg
Lifecycle:
New from this manufacturer.
Delivery:
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